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Posts Tagged ‘restoration’

Firestone 4-B-31 “Roamer” Car Radio [In Progress]

November 12, 2011 1 comment

Just a short update to show what I’m working on right now. Other priorities have gotten in the way of actually updating this site over the last week, but things are still going on in the background!

One project up on my bench is a 1951 car radio, a Firestone 4-B-31 “Roamer”. It’s a 6V radio that uses a vibrator power supply and 6 tubes to receive the AM band, and should clean up pretty nicely once it’s finished. I’m repairing this one for a client I met locally who is building a rat rod out of 1920s-1960s car parts.

 

1942 GE LF-116 Radio Repair Part 5 – Alignment and Reinstallation [Finished!]

October 24, 2011 6 comments

Part of a continuing series that is now finished – see the previous installments:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuilding
Part 4 – Capacitors and Socket Replacement 

After a brief delay while I waited on parts from my supplier, I’m finally set to finish up the GE LF-116 that I’ve been working on this month. It’s going to be returned to my office in playing shape very soon!

I powered up the radio for the first time with the power supply activated to get a feel for it, and played an MP3 through the line input. It played great – for about five minutes, until it heated up, then a nasty 60Hz hum took over. I’d let the set sit for a few minutes, then power it back on and it was fine for a minute or two before humming again. This was very clearly a thermal short, heater to a cathode. There are four tubes in the radio that are prone to H-K shorts: two 6SG7s and two 6SH7s. One of each tested totally dead, and the others were weak. So was the 7Q7 oscillator. I ended up ordering a new set of NOS tubes for the RF stages, and installed them; the radio played perfectly at this point although not very well aligned.

First, I peaked up the IF transformers with a 455KHz reference signal from my generator:

This step could be done outside of the cabinet, but the RF alignment required putting it back in and attaching the antennas.

With the installation  complete, I switch over to RF calibration, first with a 17.8MHz reference signal, then a 1500KHz, finally a 580KHz signal to align the Shortwave and AM bands.

I peak the alignment trimmers with the radio installed in the cabinet using a non-inductive alignment tool:

The trimmer locations were clearly called out on the service documents, so it was easy to find where to adjust even though it’s not the easiest to reach. It aligned up nicely! The dial tracks perfectly now. And speaking of the dial scale, it’s interesting – the tuned station is indicated by a thin line of red light surrounded by shadow.

And that’s it! Back to the office it goes. I’m not planning to do much with the cabinet as it’s not that bad, and it’s going to be in a bit of a high-traffic location so if something happens to the finish I won’t have to worry about it.

Short Project: 1940 RCA Globetrotter A-20 by John Vassos

October 23, 2011 1 comment

The last of the three radios I picked up from an estate sale a few weeks ago, I spent about an hour this evening bringing it back to life. I’m still waiting on parts for my GE LF-116 – my supplier sent me the wrong tubes – so while that’s on hold I’m checking off more projects from my list. This was the most recent one:

The RCA Globetrotter A-20 radio is a Canadian design, not sold in the U.S. but quite a few have made it south of the border over the years. It was designed by famous industrial designer John Vassos for RCA which makes it a desirable and very attractive, if not terribly well-performing, radio.

It’s a simple five-tube transformer radio with a ready input for hooking up an MP3 player or other external audio device, controlled by a switch on the back. It has interesting shortwave bands – on U.S. radios, the wave bands are usually 1.8MHz-5.5MHz and 5.5MHz-18MHz; on this one it’s 2-6.7MHz and 7-22MHz to match what the Canadians were using at the time.

The previous owner had replaced about half of the capacitors with late ’80s or early ’90s Orange Drops; I replaced five more capacitors he’d left in place as well as the electrolytic filters. Then it was time to power on and see what happened:

Powered on nicely! A bit more hum than the other sets I have, but not enough that it’s malfunctioning – it’s just a radio with simple circuitry.

It was tricky getting the dial scale back in alignment with the pointer, as the dial stays in the cabinet and a slug fits in between two pins on the pointer to move it. It took a few tries to get it aligned right, then I tapped it into place with a long-handled screwdriver.

The alignment is spot on, receiving KIXI 880 AM exactly where it should be on the dial, no further repairs necessary. Including time spent removing material from the cabinet, this was about a two hour project. I skipped a lot of the initial checks and just started working on this one, since it’s for my own collection, which cut down on the time significantly.

Short Project: A New Lease on Life for an Unknown Small Radio

October 15, 2011 1 comment

I visited a radio collector’s estate sale this morning and went home with a couple new projects. I started working on the first of them this afternoon, an incredibly simple small radio without any particular brand identification. I snapped these photos quickly while working, so they’re a little less pretty than I usually have. There’s a complete picture at the bottom!

Edit: I’ve identified this as a private-label rebranding of a 1935 Mission Bell model 35 radio.

The radio is very simple. It’s a 4-tube tuned radio frequency (TRF) type receiver with line-up 6D6 76 42 80. This is about the simplest radio you could make during the mid 1930s, acceptable if you lived in an urban area close to the radio station but not sensitive enough to pick up anything further away.

Like I said, there’s not really much going on down there. It has a total of six capacitors, five resistors, and an interstage coil.  I replaced everything that could possibly be replaced, including the fraying power cord, and added an interference suppression capacitor across the line. I changed the 4uF and 8uF filters to both 10uF, which is within the tolerance for the 80 rectifier and will eliminate a little more hum.

Powering on for the first time…a whole lot of nothing.

Turns out the output tube, the 42, was bad. I don’t have any spare 42s, but it’s basically identical to the 41 tube and I have a few of those lying around. With that substitution made, it makes sound! As you can see, I worked on this one in my kitchen with the vent hood going – the main work bench is taken up by the GE that is currently on hold pending a tube to arrive in the mail.

Back into the case. The radio itself bears a tag indicating it was built by Mission Bell in Los Angeles but the provided model, 41, does not match the Mission Bell model 41. It’s most likely a no-name contract radio sold in a neighborhood drugstore or similar.

And lit up!

Power-Volume on the left, Tuning on the right. It’s not the most exciting thing in the world, but it was a fun short project that took about 2 hours total – some of that time spent figuring out what a totally obliterated resistor was supposed to be, and finding where I’d put my stash of #41 tubes.

1942 GE LF-116 Radio Repair Part 4 – Capacitors and Discriminator/Phase Inverter Socket

October 15, 2011 4 comments

Part of a continuing series:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!

I’m continuing to work on this 1942 GE radio which I’ve been enjoying in my office for a year, and now it’s time to make it play again. I’ve pulled the chassis out of its cabinet for inspection, made a test jig, and rebuilt the multi-section can capacitor above the chassis due to lack of room underneath for mounting replacements. In this issue, I’m going through the capacitors and cleaning up a few other issues that cropped up along the way.

As we’ve already seen, there’s a fair amount going on down here. For all the empty space under this large chassis, General Electric’s engineers decided for one reason or another to use only about 1/3 of the available space and pack everything into that area as tightly as possible. There may have been some interference concerns, but I suspect a cost-saving measure for one reason or another that’s long lost to history. It does make it a lot of fun to work on, as capacitors are tucked in between the band switch, three layers deep under wiring and resistors, or otherwise made as annoying as possible to access. I’ve been spending a good bit of time with a needle-nose in each hand and that requires a special amount of coordination that makes for slow going.

This radio uses an interesting arrangement. On shortwave or AM bands, the first tube is a tuned RF amplifier helping with distant reception. On the FM band, the first tube is switched into the first stage of a cascade converter system where there’s a two-stage stepdown to the 4.3MHz intermediate frequency – this was done because at the time, tubes didn’t have the bandwidth to perform the conversion in one step without losing quality. It makes for a crowded and more complicated circuit, though, as quite a few coils are switched in and out depending on what’s being requested at the time.

The radio bears evidence of having been serviced many times throughout its life with several different brands of capacitors from varying ages, date codes ranging from 1940 up into the ’60s. There’s the usual poor soldering in a few spots, clipped component leads left on terminals, and general quick re-work but by and large it’s in decent shape and doesn’t appear to have been “hacked on” very much.

I began replacing capacitors one by one, mixing radial or axial styles depending on the location, and came to a resistor that had burned out – just to the right of the red clip I’m using as a marker.

My copy of the schematic wasn’t very readable, but another hobbyist was able to supply me a better scan and I ended up purchasing the complete set of high-resolution media as a result of seeing this sample.

With this wiring snip, the full schematic diagram, and some confirmation from another hobbyist I was able to identify the burned out resistor as R-11, 2.2K Ohms 2W, which supplies B+ voltage through IF transformer T1 to the plate of the 6SG7 converter. Capacitor C-32, a 0.02uF coupling capacitor, was shorted which passed B+ directly to ground and caused it to burn up quickly. This obviously happened at least once in the past, as C-32 was a replacement as was that resistor.

Capacitor replacement followed pretty unexcitingly, assisted by my Hakko for cleaning up terminals. I rebuilt the above-chassis capacitor block in Part 3, linked from above. It’s slow going due to the large amount of brittle, crumbling rubber wire and tight quarters. Many restorers advise either replacing or covering with heat shrink this wiring as if it crumbles, it could short out. Mine is mostly intact, and by taking extra care not to bend – just to push – the wiring around I’ve avoided having any crumbling accidents so will not be doing that time-consuming step unless it turns out later that it’s absolutely necessary.

Very unfortunately, though, a tie point snapped off the socket below the molding while trying to replace one of its connections. These loctal sockets seem more fragile than the octal sockets used in 9 of 11 tubes in the radio. I ordered a set of brand new ceramic loctal sockets from Angela Electronics who boast “Since 1977 we’ve supplied thousands of hard to find items to musicians and tube audio enthusiasts worldwide.” Hard to find no question, as they’re the only site I’ve found that sells loctal sockets – as well as brand new ceramic 5- and 6-pin sockets! On this fact alone, they’ve got all my business for new sockets going forward.

The socket arrived; I carefully remove the wiring from the terminals and drill out the rivets for the socket to replace.

Ceramic sockets are nice and durable. But, naturally, there was another issue: the mounting tabs on the 7K7 socket weren’t spaced evenly with the chassis holes AND unless I wanted to mount with rivets instead of 6-32 screws, I wouldn’t be able to get the tube to seat properly – the mounting was interfering with the base. At this point, my significant dislike for loctal sockets was solidified and I said forget it, grabbing an Octal socket from my parts bin. I mounted the octal socket above the chassis held in by the retaining clip to ensure there’s enough space to seat the tube properly.

A 7K7 tube would go into the loctal socket; for the octal socket, the same tube is labeled 6AQ7GT. I don’t have one of those in stock so ordered from eBay for $2. They’re both double-diode/triode tubes, serving as discriminator and phase inverter for the audio output. And, annoyingly enough, they’re laid out somewhat differently. Whether this was for any particular technical reason or just a rivalry between companies, I don’t know but the socket required re-wiring beyond just hooking the leads back up.

7K7(Pin) 6AQ7GT(Pin)	Description	Visual
1	 8		Heater		Grey Resistor/Ground Tie
2	 6		Triode Cathode	Orange Resistor
3	 5		Triode Plate	Orange Cloth-Cov. Wire
4	 4		Triode Grid	Orange-Drop Cap and Res.
5	 1		Diode 2		Green Cloth Wire into Can
6	 3		Diode 1		Green Rubber Wire into Can
7	 2		Diode Cathode	Cloth Wire into Can
8	 7		Heater		Black Rubber Wire to Tubes

With that mapping completed, it was time to re-wire. This required slightly extending some of the wires coming from the discriminator transformer.

This radio is by far the most frustrating to recap of any I’ve worked on yet. It might actually be the most complex one I’ve worked on so far anyway, but the construction – layers upon layers of tight components with sensitive lead dress requirements buried deep inside the radio. Much of the time I was replacing some of the deeper components with a pair of needle-nose pliers in each hand, and I even had to remove the output transformer from its mounts to replace three capacitors located basically under it.

Around the output transformer and push-pull output tubes, there were a handful of 1000V-rated 0.05uF capacitors. I don’t have 1KV metal film capacitors in stock, so I used 1KV-rated ceramic multilayer capacitors with a Z5U temperature coefficient…should be mostly sufficient for the application. Z5U-rated capacitors operate between 10C and 85C with a maximum variation of -56% to +22% capacitance, and honestly the original manufacturing tolerances of paper, foil and wax were probably broader than that in the first place.

A resistor bypassed with a capacitor. The resistor itself is a 1.2K 5% resistor, but it’s actually drifted by about 10%; I’m hoping this won’t be a significant issue but if there’s an issue around the oscillator circuit, this’ll be the first place I revisit. If I’d noticed the tolerance marking before reconnecting, I’d have replaced the resistor outright as well.

These capacitors have identical ratings – 0.005uF and 1000V tolerance. What a difference better manufacturing technology makes. The smaller physical size actually caused some mounting issues of its own, though, as the replacement component had shorter leads that required extending with a small piece of jumper wire in a few locations.

Naturally, it was bound to happen that something else would break during this process. I heated this joint with my Hakko to clear some solder, and the lug cleanly separated the instant I did so – it was held on by solder alone, it seems, the underlying metal having broken from thermal stress or a past workman’s abuse sometime during the last 69 years. Fortunately, very very fortunately, this is just a tie point – it’s not connected to the actual switching pads. I soldered a jumper to the rivet for physical stability and replaced the capacitor as normal. If this had been an active switching lug, this could have potentially permanently crippled or even rendered the radio unservicable.

Finally, I reattach the rebuilt can capacitor. I ran the common to the can’s mounting lug, then a jumper from there to a near-by ground tie point and soldered the lug to the chassis, the wire to the lug and the jumper to the lug as well. This ensures a solid ground even in the event the chassis soldering didn’t  take very well. I ended up using my Hakko as a soldering iron in this case, as the thermal mass of the tip allowed it to heat the chassis to soldering temperature without cooling; the iron I use for adding solder to most connections is a thin point that cools too quickly when heatsinked.

I did a tube-less power-up to make sure there were no immediate shorts, such as a stray piece of solder, and found that the Beam of Light lamp was burnt out. Fortunately, I have #44 dial lamps on hand:

With the radio’s electrics fully serviced, now I can continue on to the first power-up just as soon as the tube I need arrives. Stay tuned!

1942 GE LF-116 Radio Repair Part 3 – Capacitor Can Rebuilding

October 12, 2011 4 comments

Part of a continuing series:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!

I’m continuing to work on the GE LF-116 radio, an AM/pre-FM radio manufactured in 1942. We left off where I’d created a jig to hold the radio upside down because it couldn’t be mounted the way I normally do, and now I’ve started to go through and refurbish the components. I quickly ran into a bit of an issue which spawned an entire new post, which would’ve normally just two or three photos in part of a larger article: It’s cramped down there!

In the center just below the “orange drop” capacitor hanging upside down is the base of the multi-section can capacitor. Seen from the top circled in red:

This capacitor houses the first second and third filters, and the output tube’s shared cathode bypass capacitor. There’s just nowhere good under the chassis to mount a terminal strip and new capacitors, so I’m forced to actually go ahead and restuff this can with modern replacements – it’s a time consuming process I’ve mentioned not finding to be a good use of my time in the past, but necessity dictates I do it this time. This is the first can I’ve restuffed, and it didn’t come out quite as well as I’d have liked but it’s passable to anyone but a purist.

I begin by removing the leads from the terminals on the bottom of the can and marking which they came from. The body of the capacitor is the common negative for all four segments and is tied to chassis ground which makes it slightly less messy than if it were an insulated can.

The lugs are marked with a shaped cutout in the phenolic base, and the mapping is indicated on the side of the can.

In this case we have:

  • 30uF 450V (C-73A) First Filter
  • 15uF 450V (C-73B) Second Filter
  • 10uF 450V (C-73C) Third Filter
  • 20uF 25V (C-73D) Cathode Bypass
I stock 10uF, 30uF and 47uF capacitor sizes, so we’ll be using a few 10s to make this work. I’m increasing the second filter from 15uF to 20uF. Original manufacturing tolerances were on the order of +80%/-20%, so this isn’t even a noticeable increase to the radio. Regardless, most times it’s safe to increase (even up to +100%) the rating of the second or later filters with no effect, due to the current limiting of the first resistor. It’s never a good idea to put too high of a capacitor as the first filter, though, as this can raise the voltage and stress the rectifier tube leading to early failure. The modern replacements are similarly sized to the original in this case:
In blue, 30uF @ 500V, each black is 10uF @ 450V (two in parallel for the second filter), and the tiny one is 20uF @ 25V. All set. Power tools and protective equipment later we’re ready to cut the capacitor open and extract the probably-toxic guts.
Some time with gloves, an exacto knife and pliers later (this was the longest part of the process), I scraped the old parts out and disposed of them. You can clearly see the foil-dielectric layers. And the pieces of the foil I shredded to get down to a place I could grip tightly enough to rip the contents out. The entire thing was sealed in using potting tar which was annoying to deal with.
I bundle up the remaining capacitors with heat shrink on all leads, then electrical tape for double-insulation.
Then shove it all back inside the can and slide the base on, then wrap the entire thing in Gorilla tape to hold the pieces together followed by a generous helping of electrical tape.
Then, I mount it back up to the chassis. Two of the crimp points broke during the removal, but two remain and that’s just fine.
I picked colors in decreasing order of capacitance; red-yellow-brown-blue. I might mount the black common to one of the crimp lugs and solder that to the chassis, or find another mounting point. Haven’t decided that part yet. Mounted to the chassis from the other side:
It’s not the prettiest by any means – but, this is the back side of the radio that isn’t going to be looked at much, I’m okay with that.
Next article, I’ll go through replacing the rest of the small capacitors and the 7K7 socket which is damaged. I’m debating replacing it with another loctal socket, or if I want to replace it with an octal socket and a 6AQ7 tube. They’re functionally identical but have different bases. More on that later!

1942 GE LF-116 Radio Repair Part 2 – Tool Prep

October 9, 2011 4 comments

Part of a continuing series on restoring this radio: 

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!

I’m continuing to work on my 1942 GE LF-116 radio. In part 1, I showed a few photos of it and talked briefly about the history and showed some photos of the different views of the cabinet and chassis. This radio has protrusions on all sides of the chassis – screws, metal seams, switches, an RCA jack, antenna and speaker terminals, and controls in the front – there’s no viable location to do my normal mounting trick of a C-Clamp and a small piece of plywood to form a stand, suspending the radio from each end. I searched the antique radio forums for a few ideas and came up with a simple one – a thick wood base with holes drilled and dowels inserted. The holes are drilled such that the dowel will land on an empty spot on the top side of the chassis, supporting it without damaging any components while it’s being serviced upside down.

I started with a pair of 2′ x 2′ x 3/4″ plywood sheets as the base, with them glued together it makes a 1.5″ thick mounting platform – should provide plenty of stability. This GE radio’s chassis is quite heavy.

I then clamped it to the edge of my coffee table and went to get lunch while it set.

The dowels are cut to size, 16″ each. I used a mix of 3/4″ oak (stiffer) and 5/8″ depending on where the dowel would touch the radio – if there were tight clearances. Faintly visible under the dowels are the guide marks for where to drill for this particular chassis.

I randomly drilled extra holes after the original marked ones were done just on expectation of using this with other chassis. I used an oversized base for the same reason – I might work on some bigger ones eventually. It came out okay:

And all mounted up:

Now the real work can begin. It’s not perfect, but it’ll do – the 5/8″ dowels and dowel holes fit together like I want them to – slightly snugly – but either the 3/4″ dowels or my 3/4″ bits are slightly off-sized as they fit only loosely. With 8 segments supporting it (including a few in between components where it couldn’t slip out) and the c-clamp arrangement in the back fixing its horizontal position, I’m satisfied it’s sturdy enough for light repair work as I’m doing. This won’t be a permanent solution, though. Steve Strong from the OKC antique radio club makes articulated chassis holders that mount to the existing chassis bolts and rotate 360° to provide perfect control. I’ll be picking one of those up in a few weeks, but sadly after I’m done with this.

Steve, e-mail linked above, is selling these for $57.50 + shipping and they’re custom made to order.

1942 GE LF-116 Radio Repair Part 1 – History and First Looks

October 6, 2011 4 comments

Part of a continuing series:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!


I’ve had a GE LF-116 radio in my office for a while and now that I’ve started to clear my long backlog of projects it’s finally made it up to my bench. I’ve displayed it in my office holding up a monitor for a while but it’s made it onto my list of October projects.

It doesn’t look like much. Most radios after 1940 until this style died out seem to all look about the same to me. It has interesting enough features and is fairly rare, though, so it was worth preserving – AM Broadcast and Shortwave reception with a tuned RF amplifier, and early FM and a high-end audio output. Relatively few radios were manufactured with the original pre-war FM band, 42-50MHz and they tended to be high end models, this one no exception. With 11 tubes, including two 6V6GT tubes in push-pull output, a tuned RF amplifier on AM and high-fidelity system on FM.

The radio was designed at a time when television had just been invented and wasn’t widely adopted and before the U.S. became heavily involved in WW2 and domestic radio production was halted, and as I mentioned, at a time when FM radio was 42-50MHz instead of the current 88-108MHz. There was an exceptionally nasty series of court battles and “lobbyist activity” which ultimately resulted in the band being moved in June 1945 – and the first year major domestic mass production of radios returned was in 1946. A few niche-market or higher-end radios contained both bands for a very short time – like the Zenith 7H820 – but most stations on the old band quickly went bankrupt. and it was eliminated. As noted in the article, there were some physical constraints – that frequency range happens to have particularly bad interference characteristics and has been mostly abandoned today, so it’s not entirely lobbyists.

It’s important because they designed the most of the radio’s circuitry to be fairly broadly resonant – in this case, this radio is known to work up to around 99MHz of the modern FM band on strong stations by taking advantage of the 2nd harmonic of the local oscillator. There are some slightly different audio parameters between the two sets of broadcasts but the older circuitry is so broadly tuned it makes it work.

The preset buttons are labeled with local Seattle stations, although they’ve since changed frequencies over the years.

There’s a 12″ speaker driven by around 5W of power. The radio itself has 11 tubes, one of the more complicated ones I’ve tackled so far. The chassis also looks the least friendly, of course – but it’s in excellent physical condition at first glance, which will make it easier. It’s just very cramped underneath. With an 11 tube line-up of 6SG7 6SG7 7Q7 6SG7 6SH7 6SH7 6SQ7 7K7 6V6GT 6V6GT 5U4G there’s going to be lot of circuitry.

It’s also difficult to mount anything to the side of it for suspending the chassis above the work surface because of protruding screws and a sheet metal seam. I’ll have to build a new jig from an idea I read – a thick board drilled in a grid for dowels cut to length to suspend the chassis above a work surface by holding it up by the middle. It’ll cost around $20 in materials at Home Deopt, I imagine. That’ll be for the next segment. In the mean time, I’m fairly worried about this power transformer. Combined with the fact this radio came with every tube except the 5U4 rectifier, I suspect the previous owner may have damaged it by trying to plug it in – or else it just failed this way in its past life and was put into storage.

Repaired: 1960 Hornyphon Attache 61 German Antique Radio

September 30, 2011 1 comment

I’ve been working on this Hornyphon Attache 61 model W 360 A radio for a customer this month. He brought the radio over from his mother’s estate in the 1970s and it’s been sitting ever since, and came to me to have it reconditioned. German radio sets from this era are nice and elegant, this one has a blonde finish that looks like it’s nearly new especially for the age:

I’ve had this one in my shop since July but had an arrangement with its owner to hold off doing the work for a short time.

The radio uses 7 tubes, ECC85 (6AQ8), ECH81 (6AJ8), EF89 (6DA6), EABC80 (6AK8), EM84 (6FG6), EL84 (6BQ5), EZ80 (6V4). European tubes use a different numbering system, but fortunately there were US-equivalent tubes – identified by the parenthetical numbers – which I was able to find for substitutes as well. The transformer has multiple taps on the primary, so it can be used anywhere by just changing the tap setting – perfect for when it moved from Europe to the U.S.:

On the left side we see a “slug” (inductance) tuner and the output transformer; the power transformer and rectifier are on the left. This model uses a single medium-sized speaker. There’s also some evidence of physical damage in the past:

This EL84′s tip is broken off, vacuum lost, and the getter inside has turned white. There was an incorrect substitute for the EZ80, too. This radio uses an early PC board, instead of point to point wiring:

that seems to show evidence of repair to the electrolytic filter capacitor at some point in the past – most likely the ’70s.

This 22uF 350V capacitor was placed across a section of the defective can capacitor up top, but without removing the defective part from the circuit. It probably worked okay for a time, but when the failed original capacitor finally went full short, it would’ve had minimal effect. This is a “hack” repair – it probably got the radio playing again, at the time, but it wasn’t made with much attention to best practices or correctness. I removed it and returned the power supply to its original configuration during the repair.

Early PC boards are extremely fragile – both due to their construction, and the fact that they’re now over 50 years old and have become brittle. I wouldn’t have accepted this radio for work without my Hakko rework tool, which handles PCB repair quite nicely:

Fortunately, there are good schematics available and the top side of the PC board is marked with the component values and shows trace locations and ground points, even:

My customer assisted translating some of the German instructions for me, which clarified a few points. I begin by using the re-work tool on the bottom of the board:

then feed the leads through the top side of the board and re-solder to the solder pad and trace on the bottom:

Looking good!

There’s a few replaced components – but not as many on earlier radios:

Also replaced the can capacitor with two single capacitors above the chassis, routed through the holes the can used go into.

With all the defective parts replaced, it came time to power it up. It comes online okay – but no audio at all! Signal tracing produced a click when I’d tap the grid of the EL84 output tube, but the 1st AF (one section of the EABC80) tube produced no click like it should have. Turns out there were several cold solder joints – probably decades old – on the bottom side of the board around the output section. It’s possible they cracked from heat, even. The problem was fixed by a quick reflow on the joints, causing them to properly conduct electricity again.

That problem sorted, the radio roared to life crystal clear on the FM broadcast band – but on the AM band, it suffers nagging crackles that override the audio and sound bad. Unfortunately, this is a symptom of a very bad problem called Silver Mica Disease and it happens due to electromigration of the silver under a strong electric field. Silver migrates out of position and when a sufficient charge builds up it arcs across the gap, resulting in a static crash in the audio. It’s repairable if you have a lot of time, or a lot of money to pay for someone else’s time, but is widely considered not worth it. In this case, my customer decided AM radio isn’t that big of a deal to him and is comfortable keeping the radio FM-only. Take a look at the link to see what’s involved in an IF transformer repair, it’s not a simple procedure.

This radio has a neat tuning indicator, a magnetic deflection tube similar to a television CRT:

As the station gets stronger, the gap in the center narrows; when it closes fully you’re locked on station.

Reassembly is quite easy:

Reassembled, running, with the replaced tubes and replaced capacitors in a parts bag. A closer view:

The backlit dial has beautiful markings, originally for the cities in Germany and around Europe where it was located. German FM radios from this time period used a shortened FM band, so this one only tunes ~88-101MHz, instead of the full 88-108MHz used in the US.

The dials are marked in German, naturally. UKW is short for Ultrakurzwelle, Ultra Shortwave, which is the FM band. MW is short for Mittelwelle, Medium Wave, the AM Broadcast Band.

And here’s some photos of the finished product, lit up:

Now that it’s repaired, I expect the radio to give many more years of faithful service receiving music and brightening up the room it lives in.

1953 Hallicrafters 8R40 Repair

September 17, 2011 2 comments

Back in May, I dug up a Hallicrafters 8R40 from one of Seattle’s local electronics recyclers, 3R Technologies. It looked like it had been stored very well, had all the tubes, the dial strings intact, no rust to speak of and not even very much dust.

This one is a bit different from the others I’ve worked on, it’s a general coverage communications receiver as opposed to being a consumer/entertainment receiver. It’s built more sturdily, designed to be serviced more easily (down to the flip-up metal top for easy access to the tubes) and was designed with an eye for sensitivity and performance to receive ham radio signals. It receives the standard AM Broadcast Band + three shortwave bands covering most of the amateur frequencies from the 160M band (1.8MHz) down to slightly longer than 8M (44MHz). It uses 8 tubes, has a tuned RF amplifier stage and two IF stages (instead of one commonly found on consumer radios) and a device called a Beat Frequency Oscillator that means it can be used to receive Morse code, not just audio signals.

It’s really interesting to think about how capable of a device this is, given that its circuitry is of the same order of complexity of maybe a dozen transistors…about the same number a modern children’s noisemaker would have and nothing compared to the 731,000,000 transistors employed in a modern Intel Core i7 CPU.

An action shot of the underside, recapping in progress, starting from the right and working left. This radio was either built from bucket parts (unlikely, given it’s from a decent brand and wasn’t their cheapest model) or was repaired several times over its life, but always well. There were 6 different brands of paper capacitors: Aerovox, Micamold, Standard Condenser Co., Micamold, Cornell-Doublier, and El-Menco. I’ve replaced all paper capacitors with film capacitors with a uniform 630V rating ignoring the varying lower voltage ratings of the original capacitors. The small values were either replaced with 500V Mica or 1000V Disc capacitors of the appropriate capacitance.

Size comparison of old and new capacitors together.

All the old caps replaced, including the across-the-line cap (blue, top left) and the electrolytic filters (middle). I mounted a new terminal strip using a #6-32 screw through an existing hole in the chassis for two of the capacitors, and used an empty grounded lug from an existing terminal strip for the third. Some would remove the can capacitor, cut it open and re-stuff but I don’t find that to be a good use of my time.

A perspective shot showing the different components. It’s pretty busy down there!

All the replaced components. Four mica caps, one molded paper cap, 18 wax paper caps and two resistors.

So, flipping it back over for the first power-up:

First thing I noticed, the dial light is out. That’ll need to be replaced. The radio does crackle to life, though, and once I get the positions to life does weakly receive KIXI 880 in perfect alignment. But it has an overpowering volume-dependent hum and low sensitivity, missing many stations I know to exist there. We’re about six hours of hands-on labor to this point. Time for troubleshooting:

The hum is volume-dependent, which means it’s (almost certainly) not an issue with the power supply. Power supply wiring errors, like insufficient filtering due to a failed or missing filter cap, usually shows up as volume-independent hum. I’ll check the third filter capacitor, though, as it’s on a different ground lug. The radio has a Radio/Phono switch on the front which changes the audio source from the detector output (radio position) to the phono input on the back (phono position). When set to the phono position the hum disappears entirely. This indicates the problem lies in the RF section. I suspect the 6SG7 tuned RF amplifier has an internal heater-to-cathode short, which will put AC hum from the AC-powered tube heater into the DC cathode circuit. It could also be a short circuit to ground around one of the other RF tubes (converter, an IF amplifier or the detector) but I doubt this, a short around a functional tube would likely take it out entirely versus a leaking short internally.

Testing the tubes revealed they were all good. Several tested nearly new. All were identically branded Hallicrafters tubes to match the set which was even more interesting, I wouldn’t be surprised if they were the originals included when the set was sold. I relocated the ground from the above foreground electrolytic from the terminal strip to an unused solder lug but this didn’t correct the problem. Poking around, I discovered that the problem seemed to change with vibration and motion and the easiest place to see this effect was changing the position of the speaker. I initially suspected an intermittent in the output transformer (seen to the left of the black EPCOS capacitor):

but several tweaks around the transformer, including substituting another speaker, eliminated it from consideration. I desoldered the speaker leads and replaced with a bench speaker:

This didn’t fix the problem, so I reversed the modification and worked backwards from the output stage to discover that I’d missed a solder connection on the detector output. While there, I replaced two 200pF mica capacitors that were looking a little ragged for good measure.

With that repair made, I powered it up and it worked very nicely. AM comes on very well aligned with good tone and all the controls function. On the first shortwave band I picked up 5 stations but two of them are broadcast in Seattle. On the second, I picked up two copies of the BBC World Service and a news station in Spanish. On the highest shortwave band I picked up what I suspect are data signals and location beacons but no voice transmissions. These additional troubleshooting steps took about 2 hours, bringing the running total up to 8 hours of repairs.

I peaked up the IF transformers, but the RF alignment was “good enough” for me so I didn’t do a full RF alignment. This was built like a tank originally, and I didn’t need to replace any of the components in the RF sections, so it should be fine for quite a while. After reassembly, I put it up on my shelf:

Now I have a working general-coverage communication receiver. It’s right near my desk, so hopefully I’ll be able to spend some time cruising the dial and seeing what else is out there. Shortwave reception is heavily influenced by atmospheric conditions, it’s different every time!

Total project time for this one was about nine hours and consumed around $20 of on-hand consumable parts. For a parts list, see the service manual.

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