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Posts Tagged ‘capacitor replacement’

Huge and Powerful: The 1937 GE F-135 Repair Complete

January 27, 2012 2 comments

I’ve finally had the time to finish one of my long-running projects repairing GE’s most powerful radio offering from 1937, the GE F-135. I picked it up from Craigslist back in November but other responsibilities kept me from getting much done on it until the 1st of this year. Finally, after a few months waiting, it’s finished and playing!

The radio came to me complete and in decent shape for the age. It’s missing the glass for the dial, but is otherwise completely intact and the finish isn’t in bad shape despite a few scratches here and there.

This radio is the current king of my collection. The best radio GE sold in 1937, it has a lot of innovative features – early APEX hi-fi reception, dual 6L6 output tubes putting out 20W of audio to a large and rich-sounding 12″ speaker; a total of 13 tubes including a tuned RF stage, dual IF stages, separate oscillator and “station seeking” automatic frequency correction.

Under the chassis it’s in decent shape too. It looks like it has been worked on before a few times – there are some ’40s, a ’50s and a couple of ’90s capacitors installed. There’s a sticker from a Seattle-area Jukebox Repair store on the back which probably explains the more-recent repairs; I looked up the address and they don’t seem to be around anymore.

First thing first after doing the complete set of intake checks on the radio, I gave the cabinet a thorough scrubbing and hit it with Howard Restore-a-Finish and it came out beautifully. The intake checks were uneventful so I didn’t take any photos, but the power transformer, all the IF transformers, oscillator and antenna and RF coils and the speaker transformer and coils were just fine. After applying the Howard’s, it really cleaned up the fading and covered over a couple of small scratches and really brought out the natural shine on the wood.

Then I tested all the tubes and found that most were in good shape (especially the 6L6G tubes installed) there were a few 6J5 and 6K7 tubes that needed replaced. I had these in stock and so it was easy to solve that problem.

I worked on this one under my kitchen’s vent hood as it’s currently too cold to vent soldering fumes outside. The chassis stand is the right width though so that’s perfect.

Every paper and filter capacitor needed replaced, as well as nearly every single one of the resistors which had drifted as much as +100% in value in some cases. Fortunately the coils are all intact or this could’ve been a much messier repair.

I also found a couple of places where the previous repairman who worked on the set may have been dyslexic, as there were a couple places were numbered resistors were reversed – i.e. R23 being in R32′s place and so forth. I imagine that couldn’t have made it work any better, anyway. I tested and replaced going along from the bottom up as needed. These are in-progress shots, so you might see a couple places where leads aren’t trimmed or components aren’t yet soldered. All of those issues were taken care of but might not have made it into the photo series.

Small caps dealt with, it was time to replace the multi-section caps. There is a 4-section can, insulated from the chassis, mounted up top with a set of 2 filter caps and 2 cathode-bypass caps. These all ran to a hole in the chassis where they went above. I snipped the long cross-chassis leads and moved the components close to their intended locations. In this photo, I’ve replaced the 10uF cathode bypass capacitor with its replacement. I like using bipolar caps for the large-value cathode bypasses but that’s just my preference and what I keep in stock (I keep those values around for repairing crossovers in old speakers) but you could use a standard polarized capacitor there.

Here’s the totally-complete underside shot.

There’s still a matter to deal with above the chassis, though. This is an AFC radio which uses a special and complicated transformer heading into the diode which recovers the audio. And it has a small resistor which is reading double it’s value and needs replaced as well, or it won’t align right.

Then I sealed the can back up:

I hooked the speaker and pushbutton assembly up on the bench and gave it a test run – it fired up immediately and started pulling in a few stations even on the Shortwave bands. The dial was off alignment a bit though, so it was time for that.

For the alignment, I pulled up the signal generator and started with an IF alignment before going back to the RF stages. This radio has a special IF arrangement with a procedure, so I aligned the 3rd IF primary, second IF secondary and primary, first IF secondary and primary, then went back and aligned the 3rd IF secondary that feeds into the diode. Aligning that discriminator was a maddening 10 minutes spent trying to nudge the adjustment ever so slightly. My goal was to get 0V between two segments, but it approached that point at an incredibly steep slope. I managed to get it there, though.

The original 0V spec was made with a primitive meter; I’ll take 0.01 on a more sensitive modern instrument. That’s perfect IF alignment. It was definitely worth it though. Now onto the RF, which involved tweaking something like 16 trimmers in a precise order with an RF signal generator at various frequencies.

Finally, it was all set! Time to reassemble.

At this point, the radio plays beautifully and pulls in stations from all over, and I’ve added a line input to let me hook up an audio source. The hassle of the AFC calibration was definitely worth it, it’s nearly like magic to watch it work. With the switch off, the radio tunes sharply and a station comes in over just a few degrees of rotation. With the switch activated, it’s like an entirely different radio – the same station will come in across about a quarter-turn of the knob, 2 divisions in either direction from the center frequency and it will block quieter stations from interfering.

The radio sounds great with a pretty good frequency response and more volume than I know what to do with, too. The relay for the motor is burnt out, though. I missed that on the initial checks so when I went to test the pushbutton function…I got a whole lot of nothing. I’ll make another post here when I do get the motor resolved but for now I’m going to hang this one up and start playing it. This was a very fun and enjoyable project and I have a beautiful radio with a commanding presence to enjoy for many years to come.

 

1942 GE LF-116 Radio Repair Part 4 – Capacitors and Discriminator/Phase Inverter Socket

October 15, 2011 4 comments

Part of a continuing series:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!

I’m continuing to work on this 1942 GE radio which I’ve been enjoying in my office for a year, and now it’s time to make it play again. I’ve pulled the chassis out of its cabinet for inspection, made a test jig, and rebuilt the multi-section can capacitor above the chassis due to lack of room underneath for mounting replacements. In this issue, I’m going through the capacitors and cleaning up a few other issues that cropped up along the way.

As we’ve already seen, there’s a fair amount going on down here. For all the empty space under this large chassis, General Electric’s engineers decided for one reason or another to use only about 1/3 of the available space and pack everything into that area as tightly as possible. There may have been some interference concerns, but I suspect a cost-saving measure for one reason or another that’s long lost to history. It does make it a lot of fun to work on, as capacitors are tucked in between the band switch, three layers deep under wiring and resistors, or otherwise made as annoying as possible to access. I’ve been spending a good bit of time with a needle-nose in each hand and that requires a special amount of coordination that makes for slow going.

This radio uses an interesting arrangement. On shortwave or AM bands, the first tube is a tuned RF amplifier helping with distant reception. On the FM band, the first tube is switched into the first stage of a cascade converter system where there’s a two-stage stepdown to the 4.3MHz intermediate frequency – this was done because at the time, tubes didn’t have the bandwidth to perform the conversion in one step without losing quality. It makes for a crowded and more complicated circuit, though, as quite a few coils are switched in and out depending on what’s being requested at the time.

The radio bears evidence of having been serviced many times throughout its life with several different brands of capacitors from varying ages, date codes ranging from 1940 up into the ’60s. There’s the usual poor soldering in a few spots, clipped component leads left on terminals, and general quick re-work but by and large it’s in decent shape and doesn’t appear to have been “hacked on” very much.

I began replacing capacitors one by one, mixing radial or axial styles depending on the location, and came to a resistor that had burned out – just to the right of the red clip I’m using as a marker.

My copy of the schematic wasn’t very readable, but another hobbyist was able to supply me a better scan and I ended up purchasing the complete set of high-resolution media as a result of seeing this sample.

With this wiring snip, the full schematic diagram, and some confirmation from another hobbyist I was able to identify the burned out resistor as R-11, 2.2K Ohms 2W, which supplies B+ voltage through IF transformer T1 to the plate of the 6SG7 converter. Capacitor C-32, a 0.02uF coupling capacitor, was shorted which passed B+ directly to ground and caused it to burn up quickly. This obviously happened at least once in the past, as C-32 was a replacement as was that resistor.

Capacitor replacement followed pretty unexcitingly, assisted by my Hakko for cleaning up terminals. I rebuilt the above-chassis capacitor block in Part 3, linked from above. It’s slow going due to the large amount of brittle, crumbling rubber wire and tight quarters. Many restorers advise either replacing or covering with heat shrink this wiring as if it crumbles, it could short out. Mine is mostly intact, and by taking extra care not to bend – just to push – the wiring around I’ve avoided having any crumbling accidents so will not be doing that time-consuming step unless it turns out later that it’s absolutely necessary.

Very unfortunately, though, a tie point snapped off the socket below the molding while trying to replace one of its connections. These loctal sockets seem more fragile than the octal sockets used in 9 of 11 tubes in the radio. I ordered a set of brand new ceramic loctal sockets from Angela Electronics who boast “Since 1977 we’ve supplied thousands of hard to find items to musicians and tube audio enthusiasts worldwide.” Hard to find no question, as they’re the only site I’ve found that sells loctal sockets – as well as brand new ceramic 5- and 6-pin sockets! On this fact alone, they’ve got all my business for new sockets going forward.

The socket arrived; I carefully remove the wiring from the terminals and drill out the rivets for the socket to replace.

Ceramic sockets are nice and durable. But, naturally, there was another issue: the mounting tabs on the 7K7 socket weren’t spaced evenly with the chassis holes AND unless I wanted to mount with rivets instead of 6-32 screws, I wouldn’t be able to get the tube to seat properly – the mounting was interfering with the base. At this point, my significant dislike for loctal sockets was solidified and I said forget it, grabbing an Octal socket from my parts bin. I mounted the octal socket above the chassis held in by the retaining clip to ensure there’s enough space to seat the tube properly.

A 7K7 tube would go into the loctal socket; for the octal socket, the same tube is labeled 6AQ7GT. I don’t have one of those in stock so ordered from eBay for $2. They’re both double-diode/triode tubes, serving as discriminator and phase inverter for the audio output. And, annoyingly enough, they’re laid out somewhat differently. Whether this was for any particular technical reason or just a rivalry between companies, I don’t know but the socket required re-wiring beyond just hooking the leads back up.

7K7(Pin) 6AQ7GT(Pin)	Description	Visual
1	 8		Heater		Grey Resistor/Ground Tie
2	 6		Triode Cathode	Orange Resistor
3	 5		Triode Plate	Orange Cloth-Cov. Wire
4	 4		Triode Grid	Orange-Drop Cap and Res.
5	 1		Diode 2		Green Cloth Wire into Can
6	 3		Diode 1		Green Rubber Wire into Can
7	 2		Diode Cathode	Cloth Wire into Can
8	 7		Heater		Black Rubber Wire to Tubes

With that mapping completed, it was time to re-wire. This required slightly extending some of the wires coming from the discriminator transformer.

This radio is by far the most frustrating to recap of any I’ve worked on yet. It might actually be the most complex one I’ve worked on so far anyway, but the construction – layers upon layers of tight components with sensitive lead dress requirements buried deep inside the radio. Much of the time I was replacing some of the deeper components with a pair of needle-nose pliers in each hand, and I even had to remove the output transformer from its mounts to replace three capacitors located basically under it.

Around the output transformer and push-pull output tubes, there were a handful of 1000V-rated 0.05uF capacitors. I don’t have 1KV metal film capacitors in stock, so I used 1KV-rated ceramic multilayer capacitors with a Z5U temperature coefficient…should be mostly sufficient for the application. Z5U-rated capacitors operate between 10C and 85C with a maximum variation of -56% to +22% capacitance, and honestly the original manufacturing tolerances of paper, foil and wax were probably broader than that in the first place.

A resistor bypassed with a capacitor. The resistor itself is a 1.2K 5% resistor, but it’s actually drifted by about 10%; I’m hoping this won’t be a significant issue but if there’s an issue around the oscillator circuit, this’ll be the first place I revisit. If I’d noticed the tolerance marking before reconnecting, I’d have replaced the resistor outright as well.

These capacitors have identical ratings – 0.005uF and 1000V tolerance. What a difference better manufacturing technology makes. The smaller physical size actually caused some mounting issues of its own, though, as the replacement component had shorter leads that required extending with a small piece of jumper wire in a few locations.

Naturally, it was bound to happen that something else would break during this process. I heated this joint with my Hakko to clear some solder, and the lug cleanly separated the instant I did so – it was held on by solder alone, it seems, the underlying metal having broken from thermal stress or a past workman’s abuse sometime during the last 69 years. Fortunately, very very fortunately, this is just a tie point – it’s not connected to the actual switching pads. I soldered a jumper to the rivet for physical stability and replaced the capacitor as normal. If this had been an active switching lug, this could have potentially permanently crippled or even rendered the radio unservicable.

Finally, I reattach the rebuilt can capacitor. I ran the common to the can’s mounting lug, then a jumper from there to a near-by ground tie point and soldered the lug to the chassis, the wire to the lug and the jumper to the lug as well. This ensures a solid ground even in the event the chassis soldering didn’t  take very well. I ended up using my Hakko as a soldering iron in this case, as the thermal mass of the tip allowed it to heat the chassis to soldering temperature without cooling; the iron I use for adding solder to most connections is a thin point that cools too quickly when heatsinked.

I did a tube-less power-up to make sure there were no immediate shorts, such as a stray piece of solder, and found that the Beam of Light lamp was burnt out. Fortunately, I have #44 dial lamps on hand:

With the radio’s electrics fully serviced, now I can continue on to the first power-up just as soon as the tube I need arrives. Stay tuned!

1942 GE LF-116 Radio Repair Part 3 – Capacitor Can Rebuilding

October 12, 2011 4 comments

Part of a continuing series:

Part 1 – History and First Looks
Part 2 – Tool Prep
Part 3 – Capacitor Can Rebuild
Part 4 – Capacitors and Socket Replacement 
Part 5 – Finished!

I’m continuing to work on the GE LF-116 radio, an AM/pre-FM radio manufactured in 1942. We left off where I’d created a jig to hold the radio upside down because it couldn’t be mounted the way I normally do, and now I’ve started to go through and refurbish the components. I quickly ran into a bit of an issue which spawned an entire new post, which would’ve normally just two or three photos in part of a larger article: It’s cramped down there!

In the center just below the “orange drop” capacitor hanging upside down is the base of the multi-section can capacitor. Seen from the top circled in red:

This capacitor houses the first second and third filters, and the output tube’s shared cathode bypass capacitor. There’s just nowhere good under the chassis to mount a terminal strip and new capacitors, so I’m forced to actually go ahead and restuff this can with modern replacements – it’s a time consuming process I’ve mentioned not finding to be a good use of my time in the past, but necessity dictates I do it this time. This is the first can I’ve restuffed, and it didn’t come out quite as well as I’d have liked but it’s passable to anyone but a purist.

I begin by removing the leads from the terminals on the bottom of the can and marking which they came from. The body of the capacitor is the common negative for all four segments and is tied to chassis ground which makes it slightly less messy than if it were an insulated can.

The lugs are marked with a shaped cutout in the phenolic base, and the mapping is indicated on the side of the can.

In this case we have:

  • 30uF 450V (C-73A) First Filter
  • 15uF 450V (C-73B) Second Filter
  • 10uF 450V (C-73C) Third Filter
  • 20uF 25V (C-73D) Cathode Bypass
I stock 10uF, 30uF and 47uF capacitor sizes, so we’ll be using a few 10s to make this work. I’m increasing the second filter from 15uF to 20uF. Original manufacturing tolerances were on the order of +80%/-20%, so this isn’t even a noticeable increase to the radio. Regardless, most times it’s safe to increase (even up to +100%) the rating of the second or later filters with no effect, due to the current limiting of the first resistor. It’s never a good idea to put too high of a capacitor as the first filter, though, as this can raise the voltage and stress the rectifier tube leading to early failure. The modern replacements are similarly sized to the original in this case:
In blue, 30uF @ 500V, each black is 10uF @ 450V (two in parallel for the second filter), and the tiny one is 20uF @ 25V. All set. Power tools and protective equipment later we’re ready to cut the capacitor open and extract the probably-toxic guts.
Some time with gloves, an exacto knife and pliers later (this was the longest part of the process), I scraped the old parts out and disposed of them. You can clearly see the foil-dielectric layers. And the pieces of the foil I shredded to get down to a place I could grip tightly enough to rip the contents out. The entire thing was sealed in using potting tar which was annoying to deal with.
I bundle up the remaining capacitors with heat shrink on all leads, then electrical tape for double-insulation.
Then shove it all back inside the can and slide the base on, then wrap the entire thing in Gorilla tape to hold the pieces together followed by a generous helping of electrical tape.
Then, I mount it back up to the chassis. Two of the crimp points broke during the removal, but two remain and that’s just fine.
I picked colors in decreasing order of capacitance; red-yellow-brown-blue. I might mount the black common to one of the crimp lugs and solder that to the chassis, or find another mounting point. Haven’t decided that part yet. Mounted to the chassis from the other side:
It’s not the prettiest by any means – but, this is the back side of the radio that isn’t going to be looked at much, I’m okay with that.
Next article, I’ll go through replacing the rest of the small capacitors and the 7K7 socket which is damaged. I’m debating replacing it with another loctal socket, or if I want to replace it with an octal socket and a 6AQ7 tube. They’re functionally identical but have different bases. More on that later!

YAMR [Yet Another Monitor Repair] ViewSonic VP191b

September 24, 2011 1 comment

A little while ago, I picked up a set of seven LCD monitors in various states of not working  to work on repairing and maybe eventually reselling. The first one was quite easy – it just needed a wire reconnected internally and works perfectly. I grabbed the second one, a ViewSonic VP191b. It’s nothing hugely special, 19″ with two VGA and a DVI offering resolutions up to 1280×1024, a 16:10 aspect resolution.

Nothing I’d use as a main monitor, but a decent consumer device. And it turns out this one’s a little more complicated to repair than the last few I took care of.

Taking the case off, you can see the high voltage power supply which takes 12V DC and converts it to a thousand or so volts AC to power the backlights; in the center is the logic board and on the right the switching power supply.

The power supply is encased in a plastic insulator to keep it from shorting to the case.

Unfortunately, this one wasn’t in as good of shape as the others. In addition to having a few bad capacitors, it turns out that the resonant transformer is also bad (the yellow square to the right in the photo above.) If this supply lost regulation when a part failed as it was running, it could cause a nasty cascade taking out transistors, transformer windings, anything really and that looks like what happened.

The capacitors used in this model are:

  • 470uF 25V
  • 1000uF 16V x2
  • 470uF 16V
  • 120uF 400V
and a complete set from Mouser.com is only about $10 or so.

I don’t have a spare resonant transformer, and wasn’t able to locate another one online…maybe the end of the road? Nope! I checked the voltage ratings on some of the logic board components and they were all rated 16V…the rule of thumb for capacitors is you overrate their voltage by sqrt(2), or 1.414 times. These were rated 16V, so I estimated from this the logic board wants a 12V input. That’s handy, and pretty easy to supply.

I need a 12V bench supply for a few other projects I have coming up, so I ordered one from eBay. This one’s inexpensive and considerably bigger than I need, but it’ll be good in the future. The ViewSonic draws ~35W, and the eBay power supply can supply up to 120W. It came without connectors, so I hooked up a line cord socket that I’d scavenged out of a dead Ethernet switch. As always, when you’re working with electricity, take proper safety precautions – don’t touch power things while they’re energized and double-check your connections.

I’ve removed the power supply from the back so it doesn’t get in the way, then depopulated it to save the remaining good components for something else:

I ended up recovering 4 small signal transistors, a bridge rectifier, several misc. resistors and small capacitors, two choke coils, an unidentified standard transformer and an NTC thermistor.

Here’s a shot of the back with the power supply removed, ready for other connections:

For the first trial, I’ll just run jumper wires.

And let’s see…

Looks like it works! My estimate about the voltage proved correct. I mount up a terminal strip just like I do with a radio and wire the new power connection to that so it can be accessed from outside the case later. I’m using a computer power molex as the new connector as that’s what I have on hand, preserving the coloring.

Testing out one more time before reassembly:

Not bad!

It joins the ranks of my other spares I’m not sure what to do with yet:

Mission accomplished. I’ll just get it a power supply of its own, a power brick this time, and it’ll be finished! You can only tell it’s been worked on by the dangling wires hanging out the bottom.

Westinghouse LCD Repair

August 28, 2011 3 comments

After seeing the repair I made on the Samsung LCD monitor, a friend gave me a few-years-old Westinghouse LCD/TV that had quit working – it wouldn’t power on anymore. It’s a Westinghouse SK-19H210S, 19″ LCD accepting VGA or HDMI up to 1440×900 resolution (somewhat smaller than true 1080P) and can also tune ATSC and NTSC television signals to receive HDTV over the air.

It’s apparently a very known fact this one has a weak power supply – all over the web. I opened it up and grabbed the power board:

Tucked away all in the back is one capacitor that’s visibly failed, which means it’s likely several are bad or will be soon.

New parts arrived from Mouser.com:

Using my trusty Hakko, I replaced six capacitors. 4 caps in total showed signs of leaking from the bottom as well (discolored board below), 2 seemed okay but I replaced anyway because why not. I’m getting better at using the Hakko and doing this kind of PCB rework in general, the entire process from start to finish only took about 15 minutes this time.

100uF 400V
2200uF 10V
1000uF 10V
1000uF 25V x 2
47uF 50V

Interestingly (or maybe not), these bad caps were the same brand as the bad caps from the Samsung: CapXon. Obviously those have reliability problems, or are just the cheapest they could buy.

Reassembled and powered on. The first power-up would come online but drop off immediately and it was making a hissing noise; it turns out I hadn’t firmly connected the backlight leads. After fixing that, I snapped everything back into place. Consumer electronics these days aren’t made to be opened up, so the case doesn’t quite fit back together the way I’d like it to around the control panel on the side, but it’s not visible unless you look for it fortunately.

Another one fixed! This one was about $12 of parts. Looks like this one goes for around $80 these days, so I’m half-way to getting my money’s worth out of that rework station already.

My next TV repair will be somewhat more ambitious. I got this Samsung HL-P4663W, a 46″ DLP (720p) HDTV for free from Craigslist. It needs a new bulb, and some other rework, and it’ll be worth a few hundred dollars after I get it sorted. I don’t intend to keep this one (as I already have a 46″  Samsung LCD that does full HD resolution) but just to repair and sell most likely.

Adventures in Dumpster Diving: Samsung 225BW LCD Repair

August 22, 2011 1 comment

I found a Samsung 225BW LCD sitting on top of my apartment’s dumpster, and figured I’d drag it upstairs. It’s a few year old model but it’s better than the current older Dell LCD that I’ve been using (1680×1050 versus 1440×900). A quick check showed that it would power on, sort-of, but the power light would flicker constantly and there was no backlight.

I popped it open, suspecting a problem in the power supply – and turns out that was right. Several capacitors on the board were showing signs of failure. Capacitors are the main component I replace in the vintage radios but cost-cutting OEMs are often known to use caps that fail after only a few years when new to save a few cents on each part that goes out the door on new things as well. In this case their 330uF and 820uF @ 25V caps had failed and the logic board was no longer getting good power.

Modern electrolytic caps fail by bulging and leaking out the top and/or the bottom, it’s easy to see at a glance. The top two are bulging and leaking; the bottom ones are bulging only which is a bit difficult to make out in the photo.

This project is one of the reasons I bought a Hakko 472D desoldering tool. It’s made for reworking through-hole and point-to-point boards, and works by melting the solder and then applying a strong vacuum through the center of the nozzle sucking it out of the way and cleaning the connection. It wasn’t cheap, but I thought it’d be important to have one of these as I do more types of electronics hobby work. I tested it out on an antique radio and it works perfectly for the annoying old joints.

This board is pretty easy to work on, the components are widely spaced and marked.

Even though it’s not bad, I’m replacing the large main filter as well – just in case. It’s the same brand as the failed ones.

Here I’ve depopulated the bad components from the board and have placed the main filter back in position, with the old one above it for comparison.

The new caps are larger than the old ones – for the same ratings, a larger size capacitor is going to be a bit more durable. For example these 330uF 25V models:

Slid the components through the top, spread the leads to hold them in position while soldering and reattaching:

Bad planning on my part meant I forgot to take a photo of the board post-repair, but it only took about 30 minutes to do the entire thing – most of which was spent figuring out how to adjust the Hakko. And for the power-up:

Success! Back to life. This LCD goes for around $150 online even today and I’ve been meaning to add a second monitor to my desk anyway, so I’m about 1/3 of the way to recovering the cost of that desoldering station after the first project. One down, two to go….This project required 3x330uF 25V capacitors, 2x820uF 25V capacitors and 1x150uF 450V capacitor which came out to $9.83.

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